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Litigation:
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Industrial/Commercial
Sector:
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Military
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| Litigation
Case Study -- Industrial Accident |
| I have
two degrees, my first one is in General Mechanical Engineering
and my other one is an advanced degree in Theoretical and Applied
Mechanics. Having these two degrees allows me to deal with both
large structures and small machine parts.
I was brought in on a case that involved common
sense and a mechanism problem. A factory worker was cleaning a
large grinding machine, a steel table that transverses back and
forth with a big grinding wheel. This large circular wheel was
heavy and thick. The operator was cleaning this machine and the
grinding wheel came down, fell on his arm and permanently damaged
his arm so he could no longer work at his job ever again. There
was litigation against the company that made the machine and the
company that he worked for, however it was a touchy situation,
he did’t want to hurt his company because he wanted to continue
to work for them.
The problem was with a single nut that held this
whole grinding mechanism up. This nut was in a small rectangular
box that was hidden. You could not see this nut, even if you did
the maintenance on this machine. This nut just came undone, it
did’t break and fundamentally there was no way to lock the nut
in. This is not against OASHA standards, but it is not a good
design because you were not able to see the nut.
We won for 1.2 million dollars mainly against
the company that made the machine. I had to work with the individual
whom had been hurt to get his story, had to obtain drawings, and
had to have good PR with the company to be able to go in to the
factory because I had to see the machine. I worked well with the
lawyer assigned to this case; he kept bringing me in asking over
and over again about the story, phrasing it different each time,
making sure I had my story straight and I had to do several depositions.
I used simple mechanical engineering on this case; no computers
were involved. The final outcome of this case is that we won and
did not have to go to court. |
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| Litigation
Case Study -- Shop Accident |
| This
litigation case involves a situation where a part actually broke.
There was a big cutting tool that cut large holes and was mainly
used for a face of a clock where you put the actual clock mechanism
itself in. This cutting tool was heavy and used a large drill
bit that was put into a drill press. Nobody knows what actually
happened but the drill press was able to spin at a fairly high
rpm and the drill broke and sent the drill bit flying. It hit
a student right between the eyes, fortunately the sharpest part
of the bit did’t hit the eye but there was significant damage
done.
Working on solving how this accident was possible
I was able to say that if this rotated at such and such speed,
and we had such and such offset it could go flying. We were never
actually able to get the straight story, either everybody lied
or could’t remember. The suit was settled out of court, it was
not a huge win financially, but the student and mother were satisfied,
and the lawyer got his percent.
Most cases take 1 to 3 years to settle so there’s
a lot of patience required. I have been involved in 20 to 30 cases
over the years but take on no more than 3 in a year; this keeps
me out of the realm of being a hired gun. I use my expertise and
weave myself through the problem, working well with the lawyers.
I have never had a law case that was simple, there almost always
in the twilight zone. |
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| Manufacturing
Process Analysis 1 |
| In 1999
the Gas Turbine division of a Fortune 500 company, which makes
fuel nozzles for jet engines, hired me and sent me to the plant
in upstate New York because they were having a terrible rework
problem with a certain fuel nozzle. These nozzles are sort of
like fuel injections for a car but a little more complicated,
you can actually hold these units in your hand as they are about
the size of a 45 revolver. These parts were being made in 5 different
plants and at this particular plant they were making fuel nozzles,
for the big bypass gas turbine engine that is used in the 777
Boeing. These turbine engines have about 15 different kinds of
nozzles, half military, half commercial.
The problem was so bad that according to GE they
had gas turbine engines, which are quite large, sitting on the
assembly line with no nozzles (there are 45 of them in a engine)
and they could go no further. They realized that part of the problem
was involved with cracking for the weld and that is why they hired
me, as my specialty is pied, cracks, and welding.
It turns out that the real problem was the environment
in the manufacturing process. The parts were stored on carts with
their welded surface facing upward. In this area there was actually
oil dripping from the ceilings onto the parts, and even if it
didn’t drip directly onto the part there was so much in the air
that it was impossible to keep these parts clean for very long.
A second problem was the parts themselves didn’t
fit up and this was a supplier problem, however the factory could
do something with it using a welding process called ‘TIG’. This
particular process is used with argon gas to keep the weld area
clean. However, the argon was contaminated by a whole bunch of
pipes that it had to run through which were made out of the wrong
kind of material to carry that specific kind of gas.
The last thing was that they were switching operators
sometimes every 15 minutes; this was their idea of lean manufacturing.
So to begin to fix the problem what I managed to have them do
was; cover parts up so the oil didn’t drip on them, then clean
the parts extra carefully sometimes running the whole part through
the cleaning line again, kept the parts clean and then cleaned
them again just before the welding process. The accounting for
where all the parts were was not accurate, this was good for me
though because I was able to set the parts that didn’t fit aside.
We then only used the good parts that fit and we purged the argon
for 10 minutes before the welding process, this got rid of the
bad argon that was sitting in the pipes. I also had them quit
switching operators every 15 minutes, actually keeping the same
operators on the same operations for this particular nozzle. The
bottom line is after this process we went from 1 reject in 10
to 1 out of 650 being bad, that is saying basically we had no
rejections what so ever.
The company had lost 4 million dollars on this
one nozzle alone and had brought in many consultants. They all
recommended different materials and different weld times but missed
the most obvious thing. After hiring me the company quit losing
money. There were other parts of the process that had similar
problems and while I was there for the next 3 years we managed
to tackle them. The plant was smart enough to keep the same operators
working on the nozzle assembly but it ran with no interference
from engineers, as it was no longer necessary. The basic idea
was to get the big matter out of the way first so you could see
what was going on with the more refined parts. |
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| Manufacturing
Process Analysis 2 |
| While
working for the same Fortune 500 company as above there was another
plant, located in Ohio, that made heat exchanger units. There
was a brazing problem with these large heat exchangers, which
were made out of aluminum, in where there were holes being created
during the brazing process. This process is one of submersing
the whole unit into a bath of molten salt. Salt has some real
advantages for brazing but it also has a disadvantage, which is
that salt can eat a hole in the unit due to the salt causing corrosion.
They were immersing this unit into a vat of salt
for 3 minutes; which is the magic number that they had been using
for 35 years. Even though they had 50% rejection or higher using
this process they continued to use the same process for 35 years,
these rejections were horrific. The units were cylindrical in
shape, if you put your arms out and made a circle, that is about
how big around the exchanger was, and about 2 feet in height.
On the production line floor you would have all these units with
huge holes cut in them stacked up to the ceiling and they would
mark where the leak was with big red paint – it was just terrible.
They had been using this brazing process for
35 years and it was interesting though to tell within the company
if this was a recent or old problem. If it was recent that meant
something had been changed in the process and if it was old then
there was something basically wrong with how they were doing it;
half of the operators said it was ancient and the other half said
it was recent. The group that said it was old could see during
the pressurization process if there was a hole and then this part
would go in to a specific welder, this welder then would magically
weld up the hole. If you saw this process you knew there were
lots of heat exchangers coming out of the brazing process with
holes all this time, if you weren’t in the group that saw the
pressurization process then you weren’t aware of the welding being
done and thought there were no holes. So the bottom line was this
was a common problem that had been going on for 35 years and no
one had looked at the process even though they had these parts
stacked up to be welded.
I discovered that the main thing that was wrong
with the unit was that they were keeping it in the salt too long,
but the salt wasn’t actually doing anything to its corrosion.
It was the alloy, which is like the solder, would run under 3
minutes and then would cut a groove into certain parts of the
heat exchanger and the groove would create a leak. So the solution
was to cut the braze time down from 3 minutes to 1 minute.
This problem had plagued them for 35 years and
now after those 35 years, with my discovery, they have no rejections.
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| Military
Sector -- Case Study 1 |
| Most
recently I suggested to the army that they abort a certain test
program they had out at Yuma Proving Ground. My recommendation
was that we would just sit over the project and go over a simpler
type of tack that would take a whole lot less time and money without
using any computer analysis.
We had a situation with the army where there
was a bad design on a part used in the Striker Vehicle, which
are tactical vehicles for the army. The bad design basically was
with the spindle that holds the wheel on. Our military has over
300 Strikers in Iraq and 40 of them had lost wheels. There was
a possibility that if the vehicle lost a wheel in the right circumstance
somebody from our side could be killed, this was a serious situation.
There is a certain amount of coordination between
the army in this case, or the military and the government in general,
and the contractors. I have a tendency to be able to bridge that
gap between them. I was able to see that a lot of the design decisions
that were being made were only sometimes a very small part of
the solution and that the bigger part was on the manufacturing
floor where they can mess up.
The spindle for the Striker has a groove with
a curvature. At the corners of the groove the curvature was supposed
to be at least 6 millimeters in radius, and it was turning out
that sometimes it was less that 1 millimeter. It was obvious that
this was a manufacturing process, if someone would have just seen
the drawing than they would have seen that 6 millimeters is just
a little shy of what we’d like in terms of bigness, we actually
would like it bigger, the bigger the better.
Where it could have been solved 9 months ago
with less money, it only took me 2 days work to assess that all
you had to do was get rid of the surface treatment as it made
no sense to do it only for wear as there was nothing being worn
on the spindle, making the notch bigger will stop the failures.
This is a manufacturing kind of situation where I can get in and
sort through in such a way that I end up knowing some things that
the government, by itself, doesn’t get to know. |
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